Re: Blueprint Engines 383 - My Bad Experience
Quote:
Originally Posted by geezer#99
Curious if your heads have been ported. I knew of a similiar problem. The heads had a port and polish job. The guy porting the heads got a little close to the water jacket. No crack just a pinhole that only showed up when the motor was fully warmed up. A pressure test showed nothing wrong. A sonic test revealed the bad porting job.
Check it out. A possibility!!
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Heads are not ported/polished. Hey, shouldn't a hole show up in a pressure test? I thought that was the point.
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'68 C-10 SWB 383 Stroker (Sold 3/2/2013)
'87 R2500 LWB 454 TBI converted to Carb
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