Thread: Restoring Rusty
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Old 10-10-2016, 05:46 AM   #4896
Marshy
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Join Date: Nov 2012
Location: Mexico, NY
Posts: 559
Re: Restoring Rusty

The water could be explained by any number of things. Leaky head gasket, intake manifold gasket, crack in the block or when you removed the heads it got into the motor. It seems quite possible some remnants from the hone job could have caused that bearing failure though. Did you lubricate the hone at all? It seems like if it was lubed it might run down the inside of the block and get all over. If it was dry then stone and iron dust would get air born and go all over. Hopefully you have it straightened out now.

FYI
Last time I pulled my heads I used a 1/4" house with a large tapered tip from my might vac kit to stick in the head bolt hole at the rear of the engine and syphoned the water jacket down, worked great, didn't get a drop of water in the cylinders.
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'84 K10, SM465, NP208, 3.42 Gears, 33x12.5-15
GM 4 bolt 880 roller block, 062 Vortec Heads
Comp Cams XR258HR-10, MSD Street Fighter HEI
Edelbrock: Performer Intake 2116, 1405 Carb
Long tube headers, 2.5" duals to Flow Master Super 40's
Vortec Engine Build

Last edited by Marshy; 10-10-2016 at 06:01 AM.
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