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Old 11-02-2020, 05:01 PM   #719
HO455
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Join Date: Feb 2016
Location: Portland Oregon
Posts: 10,867
Re: Working Man's Burbon

OUCH!!!
My test drive didn't go as smoothly as it seemed. (Photo #1) I thought 5/16" of clearance would be enough, but obviously I was mistaken!
Doing the caster modification to the lower control arm moved the lower shock mount forward causing the problem. I had forgotten that was the reason for the shock mount modification on the old control arms.
I fabricated some new mounts. Photo 2 shows the spacer I used to set the distance between the two tabs of the mount.
Photo 3 the completed mounts. And last one of the new mounts installed with a ton of clearance. I turned the lower part of the shock 180 degrees and will run them for a hundred miles or so just to be sure nothing touches.
The upside of this is that I haven't been happy with the shocks for some time so I'm looking forward to getting better ones.
I forgot to mention I also installed new outer tie rod ends and a new Pitman arm.
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Thanks to Bob and Jeanie and everyone else at Superior Performance for all their great help.
RIP Bob Parks.
1967 Burban (the WMB),1988 S10 Blazer (the Stink10 II),1969 GTO (the Goat), 1970 Javelin, 1952 F2 Ford OHC six 4X4, 29 Model A, 72 Firebird (the DBP Bird). 85 Alfa Romeo
If it breaks I didn't want it in the first place
The WMB repair thread http://67-72chevytrucks.com/vboard/s...d.php?t=698377

Last edited by HO455; 11-05-2020 at 11:06 AM.
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