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Old 04-13-2017, 11:41 PM   #216
HO455
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Join Date: Feb 2016
Location: Portland Oregon
Posts: 10,865
Re: Working Man's Burbon

The up side of the fuel guage debacle is yesterday when I got done with the guages I wasn't sure if the fuel reading was wrong or if the new guage just displayed a lower level. I knew I was low on fuel so I went and filled the tank for the first time since I bought it. It took 15.2 gallons in the stock tank. I don't know how empty that is, but it didn't cause the guage to move. Forward to today and when I crawled under the back to check out the wiring. I found the fill hose had softened and split and now fuel was dripping steadily from it. I had been smelling gas all morning, but thought it was from this 66 427 motor that had appeared next to the WMB on the overnight. I was aware the hose was kinked and it was on the list. But just not today's list. I had to order a foot of 1 3/8" hose to get the 7" I needed. I will replace the vent hose too.
Also today I reworked the front bumpstops. The new air bags are taller when they are aired out by about 1 9/16". I scored the two red 1 1/2" bumpers at the swap meet. I installed them in the upper plate holes and added a 1/4" spacer to the lower bumpers. Then it was just a matter of drilling two new holes for the plate bolts. I'm not sure this will be a long term solution as I'm also thinking of adding some steering stops. So why not combine the two like GM did? I will have to replace the control arm bushings and ball joints at some point not to far down the road. To make that job quicker I want to get a second set of control arms, rebuild them and then its just a swap out.
I have noticed that the new air bags are touching the lower control arm when aired out. So it looks as if some modifications are needed. I did a quick check of the interweb and didn't find any lower arms with air bag clearance that were set up for a stock sway bar. I guess it's time for some more imagineering.
And thank you Advanced Design. Hot metal chips are a good reason for a big beard.
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Thanks to Bob and Jeanie and everyone else at Superior Performance for all their great help.
RIP Bob Parks.
1967 Burban (the WMB),1988 S10 Blazer (the Stink10 II),1969 GTO (the Goat), 1970 Javelin, 1952 F2 Ford OHC six 4X4, 29 Model A, 72 Firebird (the DBP Bird). 85 Alfa Romeo
If it breaks I didn't want it in the first place
The WMB repair thread http://67-72chevytrucks.com/vboard/s...d.php?t=698377
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