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Old 02-09-2014, 03:16 PM   #38
67Steven
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Join Date: Mar 2007
Location: Oregon City
Posts: 228
Re: 1972 K5 4x4 modified build

Well, I tried and tried to start it, but it would just backfire. After going round and round with PSI, I decided to use the original harness, which is what I should have done in the first place.

Since the harness is from an H2 Hummer, the ECM needed to be mounted in the engine bay. So I bent up a new one to sit on the driver’s inner fender:



I took pics of the wiring I was extending so I wouldn’t screw it up:



I then extended the wiring for the fuses into the tub and mounted it above the throttle pedal:


I was ready to start it, but I read I should clean the injectors, so I did. This is what came out of the fuel rail when I took it apart. And it STUNK. I still don’t know what it was:


Put it back together and it fired right off! I was pumped.

Here is the ECM mount in the bay:

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