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Old 09-02-2012, 11:06 PM   #38
Shaun1162
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Join Date: Aug 2010
Location: NH
Posts: 368
Re: Late 60's Vintage Modified Race Car

Had some more time yesterday and this afternoon. Dropped the motor/trans in. Went pretty good considering I did it by myself, I've only done it once before and I only had a regular car lift to do it with.





I guess I know why they torched that section of the frame out now..



So I've been thinking that this car last ran with a 3 speed out of an F1 because of the transmission crossmember they built had two holes close together. But after getting the rear mount, it wasn't even close. But then I got to looking at the other mount they had where a bolt was sticking up and it looked close and of course this trans bolted right to it. Looks like they cut out the other side of the mount for some reason..

But if anyone has any idea what other transmission it might have had I'd be curious to know.. The crossmember sit back maybe 2 or 3" from the end of this F1 transmission, and the only two holes for bolts are in the center maybe and inch or two apart. I'll try to get pictures tomorrow of it to help with ID..



So I had good luck with the one transmission mount, but the motor mounts were a different story...





Any ideas what might have cause this? Is it because it's an 8ba instead of the older style flatheads? Or maybe they had a transmission that set back a little more?

There was also a fitment issue on the driver side by the steering box...



Looked like quite a tight fit for even a stock manifold let alone headers

But then I remembered that with the rubber mounts it'll probably sit up another 1" or so which would help.

So I took out the motor mounts that were in it thinking I'd have to make some new ones, but then I held them against the frame and moved them forward about and inch to line up with the water pump holes and it looked like they'd fit. So I got out the welder and welded them to the frame but not permanent so I could rework them if I had to. I was able to get the rubber mounts in after that so it looks like those motor mounts will end up working in that position

(Had to go out and get a new engine crane of course )



Hard to tell from the picture but I gained quite a bit of clearance by the steering box. The dipstick tube still hit the box but just barely so I'm sure something could be done about that.




Looks like the radiator might be a tight fit......

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